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INVESTIGATION OF NOISE FROM FULL-SCALE HIGH BYPASS ENGINE AND BLOWN FLAP SYSTEM NASA - Lewis Research Center
- Format:
- Conference/Event
- Author/Creator:
- Jones, W. L., author.
- Conference Name:
- National Air Transportation Meeting (1974-04-30 : Dallas, Texas, United States)
- Language:
- English
- Physical Description:
- 1 online resource
- Place of Publication:
- Warrendale, PA SAE International 1974
- Summary:
- A summary is presented of an acoustic test program for investigating engine noise suppression and jet/flap interaction noise associated with an EBF STOL powered lift system. A highly suppressed TF-34 engine and EBF wing were used in the investigation. The engine was suppressed 21 PndB to a level of 94 PndB. An UTW powered lift system was tested with conventional, mixer, and decayer-type nozzles. The configuration with velocity decayer nozzle and acoustically treated shroud had the lowest noise (98 PndB). An OTW configuration with non-decayer nozzle was about 10 dB quieter than the corresponding UTW system. UTW and OTW noise data are compared with scale model correlations
- Notes:
- Vendor supplied data
- Publisher Number:
- 740467
- Access Restriction:
- Restricted for use by site license
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