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INVESTIGATION OF NOISE FROM FULL-SCALE HIGH BYPASS ENGINE AND BLOWN FLAP SYSTEM NASA - Lewis Research Center

SAE Technical Papers (1906-current) Available online

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Format:
Conference/Event
Author/Creator:
Jones, W. L., author.
Conference Name:
National Air Transportation Meeting (1974-04-30 : Dallas, Texas, United States)
Language:
English
Physical Description:
1 online resource
Place of Publication:
Warrendale, PA SAE International 1974
Summary:
A summary is presented of an acoustic test program for investigating engine noise suppression and jet/flap interaction noise associated with an EBF STOL powered lift system. A highly suppressed TF-34 engine and EBF wing were used in the investigation. The engine was suppressed 21 PndB to a level of 94 PndB. An UTW powered lift system was tested with conventional, mixer, and decayer-type nozzles. The configuration with velocity decayer nozzle and acoustically treated shroud had the lowest noise (98 PndB). An OTW configuration with non-decayer nozzle was about 10 dB quieter than the corresponding UTW system. UTW and OTW noise data are compared with scale model correlations
Notes:
Vendor supplied data
Publisher Number:
740467
Access Restriction:
Restricted for use by site license

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